Huabei Oilfield Fourth Factory multi-pronged approach to increase energy-saving emission reduction efforts

According to China Petroleum Daily, the first 11 months of this year, Huabei Oilfield 4 Power Plant consumption dropped 6% over the same period last year, and conducted a pilot heat pump solar test, which is the plant made another new progress in energy-saving emission reduction. The plant through the improvement of long-term mechanism to build resource conservation, technological innovation, promote the use of energy-saving products and other effective measures to save energy and reduce consumption throughout the job details, forming a "low investment, low consumption, low emission and high efficiency" Economical economic growth mode, was Huabei Oilfield as "winning energy-saving labor competition unit" and "energy-saving advanced unit." In order to enhance the awareness of energy conservation and consumption reduction of all employees, the plant has stepped up publicity and education on energy conservation by popularizing knowledge banners, relying on websites, board newspapers and holding labor contests and other carriers to popularize knowledge on energy saving and consumption reduction, , Solar terms, fuel-efficient as the main content of the "four" practice. Actively promote civilized energy-saving work habits among employees, to create a "good atmosphere for everyone to talk about saving energy, everything wants energy saving". The factory did a good job of system efficiency testing, the whole plant pumping unit, injection pump, heating furnaces and lines for energy consumption testing. Based on the test results, decision-making departments make timely comparative analysis, scientifically adjusting and optimizing equipment operating parameters to improve system efficiency and ensure high-efficiency and low-cost operation of the equipment. The factory regulates the management of refined oil products, reduces fuel consumption, standardizes and unifies the registration system of accounts, conscientiously checks the fuel consumption with all units, and implements the cardholders and the number of cards held by each unit. Through careful deployment, self-use oil conservation effect is very significant, refined oil management has made progress. The factory has also implemented the measures of saving energy and reducing consumption to first-line production through such measures as perfecting the mechanism of resource conservation, promoting technological innovation and promoting the use of energy-saving products, and formed a "low input, low consumption, low emission and high efficiency" Economical mode of economic growth. In the first half of this year, the factory completed the energy consumption test of 177 pumping units, 22 pump sets, 10 heating furnaces and 7 power lines; installed 10 sets of waste heat recovery equipment for natural gas generators and reasonably controlled the parameters of the heating furnace; Annual savings of 1.5 million cubic meters of natural gas; in Beijing 69, Springs 75-5, State 21 three single well pull-point installation of solar heating devices, is expected to save 543,000 tons of standard coal; replace energy-efficient transformer 81 units, inverter 20 units, 18 sets of high-voltage compensators and 120 sets of low-voltage compensators. It is estimated that it will save 2.65 million kilowatt-hours annually. The plant to strengthen energy saving process management, to ensure efficient operation of equipment, and constantly explore the law of daily production of oil wells, the oil wells and empty wells with less open form, to reduce unnecessary waste of energy, has implemented more than 100 wells Between the open, from the original open 24 hours to 8 hours, saving more than 4,000 kilowatts hours of electricity; by laying water pipelines, the excess sewage treatment back injection, reducing the amount of water, cost savings of more than 30 million.